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  1. #11
    This is what i'm battling:

    https://photos.app.goo.gl/32mNoD2Wcsz9pnzEA

    Note letter W in my text speed tests. Even straight angled lines getting the wobble.
    Circles (or spirals in my tests) exhibit same vibration patterns radiating out from the centre of ALL cut tests.
    The accelleration has been knocked down in half from factory defaults, lowering them any lower makes machine sluggish and controlling tube power becomes an issue (sharp corner overburn, slow decelleration/accelleration induced).

    What has been done to day:
    1. Replaced super-thin and warped table raising brackets to more substantial and 2 point mounted ones.
    Initially, the table was held up by a single m4 screw in a hole drilled for m5 and covered with wider washer to cover size difference. Original brackets got bent on tightening washer nuts. Table subframe had m5 holes drilled from underneath, for TWO mounting points, but only ONE access hole on the other size. As i said, only mounted by one undersized screw.

    2. Replaced original 1.5mm aluminium head mount plate to 2mm steel, laser cut by my friend at his workplace. they cut steel for screeners/heavy machinery, plasmas and lasers. Laser in my case as i had small mounting holes and some that needed tapping. Plasma cant do fine detail, hence laser. Had to pull the part, caliper it around and draw out the part for cutting (used to work with autocad a lot, so no biggie). Helped, but only marginally. Wobliness didnt go away.

    3. Tested for Y rail vibration transmission. Moved the head to work position in the middle of the table, loaded a 100x100 test pattern (spiral), lightly clamped Y rail to the frame - most of wobliness went away.
    Didnt want to wreck existing rail by clamping/bending it, so didnt do any more tests after that. Its pretty damn convinced me to replace whole Y "assembly"...

    4. Bought SBR20 rail and double cartridge bearing (95mm long). Cutting the rail was a bit of a challenge, as NONE of local engineering companies had abrasibe cutting machines. All of them mostly work with mild steel, so bandsaws or reciprocating saws only. The hardened rail would have wrecked anything with teeth... I cut off a piece for gantry height fitting by an angle grinder. Disk wouldnt reach all the way through 20mm, had left about 3mm, wrecked 3 bimetal blades in my hand hacksaw to finish the job... Yeesh...

    5. Designed and laser cut mounting plates for connecting gantry to bearing. Asked to cut in all available thicknesses from 8mm to 2mm as exact measuring is tricky, all of the machine case is welded, caliper wouldnt fit. So i decided to do a "sandwitch approach" - pick most suitable thickness of 2 plates and weld them before fitting (when it fits correctly.). The idea was to put one plate on the bearing and one plate on gantry, without disturbing existing hole patterns on gantry, which required me to split mounting plate in two due to existing gantry holes. Shim it as necessary. All of this is being done to prevent any disturbance of mirror 1 and the tube placement. If i move one of those - lots of pain of readjusting the whole beam path, squareness issues.

    6. Removed all MXL belts and pulleys and replaced them with GT2 10mm belts/pulleys. I highly suspect Y pulleys fitted are GT2, which is a mismatch, as MXL is 2.032 and GT2 is 2mm pitch. Original belts were also too short, at slackest (tensioner all the way inward) they ring. New belts will be about 10mm longer for this reason.

    7. Replaced MXL belt with GT2 10mm on X motion (head on the gantry). Had to replace motor as it had pulley pressfit onto it and too short a shaft to fit GT2 pulley with set screw on. Also, while doing tests i have noticed that X motor was getting too hot in XY operations, but, interestingly, NOT in engraving where its moving the most. For some reason, doing vector engraving, while both motors run equally as much, only X was getting overheating. Y, while carrying the whole gantry/head/Xmotor assembly would barely rise in temperature at all... go figure.

    8. As someone suggested i swapped over both stepper drivers just to see if overheating issue would move to Y axis - it didnt. Both drivers are functioning. However i still cannot identify them. They are marked as M415DRV, but there is absolutely nothing about them on the t'intertubes... Bought DM556 drivers, for now they sit on shelf until i finish Y rail and gantry assembly.
    Cannot do same swapping test on motors, as Y motor is dual shaft and both ends needed to drive Y, while X is single shaft.

    9. By chance came across and bought some Baldor integrated motors, 3 nema17 and one nema23 sized. Not encoded ones, but with drivers built into back housing. Will be using nema23 one to drive Y later as i'm planning to chuck that welded in nema17 bracket out. Need to figure out the 2:1 recduction for Y single shaft. Have to design it first, but thats for later.

    10. I even suspected my room floor having something to do with all this vibration in cuts nonsense, soft floor (insulation etc). So i moved the whole machine into bedroom where i have tiled section sitting on concrete slab - no change, same vibration patterns in cuts, so no external vibration transferrence...

    At this point i'm focused on replacing original 12mm hanging rail with supported 20mm rail. After that, when i verify problem gone/not gone, replace extraction (one more thing that may have induced vibration as its built into the case, that thought came after i started Y rebuilding), insulate high voltage wiring with silicone tubing, replace both motors with known specs, replace both drivers or use Baldor integrated ones i got by chance. Design/manufacture switch/indicator console for water/air/power meter/lighting/accessories. Clean up wiring, as at the moment power wiring is sitting in the same trunk as signal/control wiring (separated for now, to rule out EM interference, was not the case)...

    Oof, long post. Are you seeing photos i shared ? There are much more, or, if you want to see something specific in more detail i can snap some more...

    #EDIT1# 11. Replaced rubbish water and air pump outlets that would not hold plugs and spark. Put on proper UK double switched socket outlets with proper grounding etc...
    Last edited by threedee; 01-08-2019 at 05:01 PM.

  2. #12
    Completely random thought, feel free to disregard...

    Is it worth placing a red laser in front of the tube and verifying the complete optical path (bit of smoke, video camera) to make sure the axis drives aren't causing vibration in the various path mirrors etc. What I'm thinking is position Y at min/max extremes and rapid transits across X, observing any oscillation in the optical path. Might be worth if only to disregard this effect.

  3. #13
    X is behaving on its own. I did multiple different scan engravings with no adverse effects. No vibration until Y axis engages. If it is only used to move a scanline it doesnt show at all. But try to cut vectors - bang, vibration all over the travel path...

    Also, i have checked mirrors for wobbling/rattle - everything is tight and screwed down. All the way along the beam path, from lens to tube itself...
    Last edited by threedee; 01-08-2019 at 07:13 PM.

  4. #14
    What is powering all this setup? It must be PSu problem. Buy a proper industrial PSU, even from China, say Meanwell at least. A no name PSU=Crap 100% of the time
    Last edited by Boyan Silyavski; 02-08-2019 at 11:36 AM.
    project 1 , 2, Dust Shoe ...

  5. #15
    Quote Originally Posted by threedee View Post
    This is what i'm battling:

    https://photos.app.goo.gl/32mNoD2Wcsz9pnzEA

    Note letter W in my text speed tests. Even straight angled lines getting the wobble.
    Circles (or spirals in my tests) exhibit same vibration patterns radiating out from the centre of ALL cut tests.
    The accelleration has been knocked down in half from factory defaults, lowering them any lower makes machine sluggish and controlling tube power becomes an issue (sharp corner overburn, slow decelleration/accelleration induced).

    What has been done to day:
    1. Replaced super-thin and warped table raising brackets to more substantial and 2 point mounted ones.
    Initially, the table was held up by a single m4 screw in a hole drilled for m5 and covered with wider washer to cover size difference. Original brackets got bent on tightening washer nuts. Table subframe had m5 holes drilled from underneath, for TWO mounting points, but only ONE access hole on the other size. As i said, only mounted by one undersized screw.

    2. Replaced original 1.5mm aluminium head mount plate to 2mm steel, laser cut by my friend at his workplace. they cut steel for screeners/heavy machinery, plasmas and lasers. Laser in my case as i had small mounting holes and some that needed tapping. Plasma cant do fine detail, hence laser. Had to pull the part, caliper it around and draw out the part for cutting (used to work with autocad a lot, so no biggie). Helped, but only marginally. Wobliness didnt go away.

    3. Tested for Y rail vibration transmission. Moved the head to work position in the middle of the table, loaded a 100x100 test pattern (spiral), lightly clamped Y rail to the frame - most of wobliness went away.
    Didnt want to wreck existing rail by clamping/bending it, so didnt do any more tests after that. Its pretty damn convinced me to replace whole Y "assembly"...

    4. Bought SBR20 rail and double cartridge bearing (95mm long). Cutting the rail was a bit of a challenge, as NONE of local engineering companies had abrasibe cutting machines. All of them mostly work with mild steel, so bandsaws or reciprocating saws only. The hardened rail would have wrecked anything with teeth... I cut off a piece for gantry height fitting by an angle grinder. Disk wouldnt reach all the way through 20mm, had left about 3mm, wrecked 3 bimetal blades in my hand hacksaw to finish the job... Yeesh...

    5. Designed and laser cut mounting plates for connecting gantry to bearing. Asked to cut in all available thicknesses from 8mm to 2mm as exact measuring is tricky, all of the machine case is welded, caliper wouldnt fit. So i decided to do a "sandwitch approach" - pick most suitable thickness of 2 plates and weld them before fitting (when it fits correctly.). The idea was to put one plate on the bearing and one plate on gantry, without disturbing existing hole patterns on gantry, which required me to split mounting plate in two due to existing gantry holes. Shim it as necessary. All of this is being done to prevent any disturbance of mirror 1 and the tube placement. If i move one of those - lots of pain of readjusting the whole beam path, squareness issues.

    6. Removed all MXL belts and pulleys and replaced them with GT2 10mm belts/pulleys. I highly suspect Y pulleys fitted are GT2, which is a mismatch, as MXL is 2.032 and GT2 is 2mm pitch. Original belts were also too short, at slackest (tensioner all the way inward) they ring. New belts will be about 10mm longer for this reason.

    7. Replaced MXL belt with GT2 10mm on X motion (head on the gantry). Had to replace motor as it had pulley pressfit onto it and too short a shaft to fit GT2 pulley with set screw on. Also, while doing tests i have noticed that X motor was getting too hot in XY operations, but, interestingly, NOT in engraving where its moving the most. For some reason, doing vector engraving, while both motors run equally as much, only X was getting overheating. Y, while carrying the whole gantry/head/Xmotor assembly would barely rise in temperature at all... go figure.

    8. As someone suggested i swapped over both stepper drivers just to see if overheating issue would move to Y axis - it didnt. Both drivers are functioning. However i still cannot identify them. They are marked as M415DRV, but there is absolutely nothing about them on the t'intertubes... Bought DM556 drivers, for now they sit on shelf until i finish Y rail and gantry assembly.
    Cannot do same swapping test on motors, as Y motor is dual shaft and both ends needed to drive Y, while X is single shaft.

    9. By chance came across and bought some Baldor integrated motors, 3 nema17 and one nema23 sized. Not encoded ones, but with drivers built into back housing. Will be using nema23 one to drive Y later as i'm planning to chuck that welded in nema17 bracket out. Need to figure out the 2:1 recduction for Y single shaft. Have to design it first, but thats for later.

    10. I even suspected my room floor having something to do with all this vibration in cuts nonsense, soft floor (insulation etc). So i moved the whole machine into bedroom where i have tiled section sitting on concrete slab - no change, same vibration patterns in cuts, so no external vibration transferrence...

    At this point i'm focused on replacing original 12mm hanging rail with supported 20mm rail. After that, when i verify problem gone/not gone, replace extraction (one more thing that may have induced vibration as its built into the case, that thought came after i started Y rebuilding), insulate high voltage wiring with silicone tubing, replace both motors with known specs, replace both drivers or use Baldor integrated ones i got by chance. Design/manufacture switch/indicator console for water/air/power meter/lighting/accessories. Clean up wiring, as at the moment power wiring is sitting in the same trunk as signal/control wiring (separated for now, to rule out EM interference, was not the case)...

    Oof, long post. Are you seeing photos i shared ? There are much more, or, if you want to see something specific in more detail i can snap some more...

    #EDIT1# 11. Replaced rubbish water and air pump outlets that would not hold plugs and spark. Put on proper UK double switched socket outlets with proper grounding etc...
    They have good ides but their attention to detail is poor. I had to rebuild my 6040 cnc router to make it work properly. And when i upgraded i just built my own machine:)

  6. #16
    Quote Originally Posted by Boyan Silyavski View Post
    What is powering all this setup? It must be PSu problem. Buy a proper industrial PSU, even from China, say Meanwell at least. A no name PSU=Crap 100% of the time
    You mean low voltage power supply ? I need to check the name. Checked voltage on it, its holding at 24V while operating.
    As for high voltage its Zye MYJG-100W. That has absolutely nothing to do with motion at all.

    Quote Originally Posted by ericks View Post
    They have good ides but their attention to detail is poor. I had to rebuild my 6040 cnc router to make it work properly. And when i upgraded i just built my own machine:)
    That is exactly what i thought and will do myself. As for having good ideas - hell no, in this case its an astonishing display of cost related corner cutting and nothing else...

  7. #17
    I have also been looking at lasers.....basically also decided to build my own. We have a small trotec laser here at work, they paid $35000 aud for it. Let me tell you there is nothing in it to justify the price

  8. #18
    35k Aud for a small laser, yikes.

    But, yeah, there is absolutely nothing in there that justifies the price. Not even tech support.
    What is laser cutter anyway... 1 tube, 2 power supplies, 1 controller, 2 motors, 2 motor drivers, some switches and wiring in a box. With what i know now i wouldnt have even entertained the idea of importing manufactured laser. Even if i didnt pay for it 35k, i would have built it for one third or half of money i paid... Bloody annoying... Got a nice case though :D

  9. #19
    This image says a lot...

    Click image for larger version. 

Name:	Screenshot 2019-08-02 at 13.32.54.png 
Views:	339 
Size:	2.79 MB 
ID:	26141

    It's unclear from some of the other pictures, but this one is particularly interesting as it would appear to show the distortion on spokes projecting radially from the spiral centre, and at a position where the Y axis velocity is tending to zero or accelerating from zero. Is this true of other images? (they are less clear).

    Could this be related to torsional elasticity of the couplings/Ali extension bars on the Y-axis?, is it worth trying to drive the two belts separately with two steppers, and removing the length of Ali bar?

    Just a random thought

  10. #20
    Yes ours at work also has a very nice rounded case and a small stand:)

    Obviously they would come out for repairs/maintenance but it's going to cost heaps!!

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