. .

Threaded View

Previous Post Previous Post   Next Post Next Post
  1. #1
    Okay, it's been a few weekends of work but finally got my SX2.7 under power...

    https://youtu.be/9T3QncRvuR4

    Bench was the original frame for a router I'd intended to build, but chickened out (it was going to be too large for the shed... so became a pretty handy bench). As part of that original design I'd planned around supporting 2 19" racks - using one of these to fit a HP server, the control box (PSU steppers, motion controller) and a server keyboard/monitor - for which the backlight on the monitor finally failed today...

    Click image for larger version. 

Name:	IMG_2273.jpg 
Views:	498 
Size:	182.4 KB 
ID:	25777

    The other 19" bay (out of shot) now simply holds my compressor (a silent 25l ex-dentist job). The central bay just holds stock material.

    Click image for larger version. 

Name:	IMG_2277.jpg 
Views:	541 
Size:	123.3 KB 
ID:	25778Click image for larger version. 

Name:	IMG_2262.jpg 
Views:	742 
Size:	129.8 KB 
ID:	25779

    Z Axis - it's all been done before, I'm just copying others who've converted their 2.7s. Z is by far the easiest axis and the original ball nut holder takes a standard 1605 ball nut. 2:1 belt drive as a general approach to all axis.

    Click image for larger version. 

Name:	IMG_2275.jpg 
Views:	712 
Size:	276.6 KB 
ID:	25780Click image for larger version. 

Name:	IMG_2279.jpg 
Views:	624 
Size:	303.8 KB 
ID:	25781

    Some detail on X - ignore the hack job on the ball nut - I was trying to expose the nut holder's bolt hole in situ to unbind the screw that was slightly misaligned after I'd tightened all bolts. That was a difficult few minutes with a Dremel and none too pretty.

    Click image for larger version. 

Name:	IMG_2276.jpg 
Views:	608 
Size:	343.1 KB 
ID:	25782

    Y Axis - very much like the others. I'm not sure that I like the limit switch so exposed, so might re-do this once I regain my enthusiasm.

    Control box is a 800VA 50V dual secondary toroidal transformer; rectifiers and 10,000uF/160VDC caps. With bleed resistors - despite arguments on here to the contrary. Stepper drivers are 2DM860H (4 of to support a 4th axis), Steppers are 3.1Nm 4-wire - just cheap eBay jobs. Motion controller is an UC300ETH with a standard parallel BOB. I finally found a use for the 5/24V PSU that I'd stripped out of a laser printer.

    Both Y and Z axis the screws are unsupported, X has a phosphor-bronze bush to support the end of the screw (butchered with a band saw) mounted in the end plate. General approach was limited to hand tools or what I could fit on a Denford Starmill (150x80 table area - somewhat limits options). Oh, and everything with an option to recover the machine back to the original manual control if necessary.


    I've tested the machine at 1000mm/min and it's faultless (I shouldn't say that so soon), though my original wet-finger - I didn't realise that UCCNC defaulted to 20% jog speed, and at one point had it running at 4000mm/min - sounded sweet but that's crazy fast for a mill this size, so it's now got a more sensible limit,.

    Next is to sort the limit switches properly then consider belt guards for each axis. I've also removed the neutral switching on the e-stop and used the now spare way of the switch to provide the e-stop signal back to the control box. This, and the probe and limit sensors to be routed through a connector mounted into the 8x4" plate on the top/rear of the column.

    What I don't have is a solution for the spindle - I've eyeballed the brushless motor controller, think I understand the basic operation but don't fancy reverse engineering that one. I might instead scope the control board in the pendant and see if I can create a closed-loop emulation of the control buttons to get a form of speed control. For now, manual operation of the spindle. I'd be interested if anyone else has a solution for this.
    Last edited by Doddy; 13-05-2019 at 06:55 AM.

Thread Information

Users Browsing this Thread

There are currently 1 users browsing this thread. (0 members and 1 guests)

Similar Threads

  1. BUILD LOG: Sieg SX2.7 CNC conversion
    By Edward in forum DIY Mill Build Logs
    Replies: 23
    Last Post: 11-06-2019, 03:01 PM
  2. Sieg X3 Conversion
    By Vikash in forum Milling Machines, Builds & Conversions
    Replies: 8
    Last Post: 04-01-2016, 05:18 PM
  3. CONVERSION: Need some help with a new SIEG SX2 Plus CNC Conversion
    By Onocyclone in forum Conversion Build Logs
    Replies: 22
    Last Post: 17-09-2014, 01:00 PM
  4. Sieg sx2 conversion kit
    By Goldigger in forum Milling Machines, Builds & Conversions
    Replies: 3
    Last Post: 24-04-2011, 07:42 PM
  5. FOR SALE: Sieg X2 Long bed + Milling vice -- SOLD--
    By rnr107 in forum Items For Sale
    Replies: 0
    Last Post: 06-10-2010, 01:04 PM

Bookmarks

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •