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  1. I've started making some of the parts for the MK4 machine. Thought I'd start with an easy and relatively quick one.
    Here is the Z ballscrew lower bearing bracket. The standard bearing bracket is too large to fit in so I've made my own again. I'll re-use the ballscrew and bearing from the MK3 machine which is already turned down to 6mm shaft at the end allow a pretty small bearing to be used. Just needs a new housing to suit the new design:

    Laying it out and machining the bearing pocket:
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    Machining the profile leaving tabs to hold it:
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    Cleaned it up and set up to cnc machine the M8 pilot holes (note that this is a drill press vice - a proper precision vice is on my wishlist !)
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    Started the taps off in the drill press (just to get them straight):
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    Then finished them off in the vice with the hand tap wrench:
    Since I discovered these lovely spiral fluted taps there is no going back . . .
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    Chamfered the thread entry with my favourite snail countersinks, then cleaned out the threads with a bolt:
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    Done:
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    More to follow . . .
    Building a CNC machine to make a better one since 2010 . . .
    MK1 (1st photo), MK2, MK3, MK4

  2. Next part is the Z axis stepper motor bracket.

    Laying it out:
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    Machining the pocket - no adaptive toolpaths I'm afraid so about 1 hour to machine this:
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    Then the slot for the motor shaft:
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    Small pocket to clear the boss on the front of the stepper:
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    Light skim to get a level surface:
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    Outer profile cut:
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    I had problems here as I had the tool stick when it was about 10mm into the part. It was on one of the curves (which I think increases the chip load a bit) and I had about 2 seconds to go from hearing the problem developing to the spindle stopping rotating. I cleared the tool and thought I'd got away with it but it had obviously missed some steps as there was a ridge in the part. I let it finish, going easier on the feedrate, then homed the machine and ran some new full depth toolpaths working up to about a 0.5mm offset inward. This made the outer surface 0.5mm smaller all round, but at least it was smooth again. For this part it did not matter so I was lucky.

    Machining the bolt slots was pretty quick:
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    Set it on end and machined the clearance holes for mounting (thought this might vibrate but it was fine):
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    Skimmed the other side down to get the final 20mm thickness:
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    That will do !
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    OK, so it was not 20.00 everywhere . . . !
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    Counterbored to 9mm deep (DRO coming in handy here to get them to the same depth)
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    Snail countersink to finish off (love these things, so much better than the star type which are a waste of time):
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    Done. Worked out OK in the end:
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    Building a CNC machine to make a better one since 2010 . . .
    MK1 (1st photo), MK2, MK3, MK4

  3. Next part is the Z ballnut bracket. All started well . . .

    Laying it out
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    Pilot holes for the threaded holes:
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    Skim the surface to level it:
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    Machine pocket to house ballnut:
    (Toolpaths are fairly basic from Cut2D - gentle ramp into material, then a series of simple circles. No spiral option. But it gets the job done.)

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    Profile machined most of the way through leaving a bit holding it in place:
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    All holes drilled to size, tapped, then on the very last hole backing the tap out - it snapped ! Aargh!
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    Tap was 12mm into the part and bashing and picking was not working. Flatten the end off the centre punch so that was no good.

    Got some Alum powder (about £3.50 off ebay for 2x100g) and mixed up a solution with hot water:
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    Then dropped in the part, and you can see it bubble straight away (bottom right hole).
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    After a day there were lots of black specs and a general browny dust settled onto the part (hole now top left).
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    But even after a couple of days it had only eaten about 0.5mm groove in the top of the tap. At this rate it was going to take weeks.

    I tried a masonary bit (3mm tungsten carbide tipped) on a very low speed in the pillar drill and this gnawed away at it for about 15 minutes. The drill kept trying to wander off into the aluminium at the sides, so I flipped the part over and put the drill bit into the hole hoping this would guide it. It made a sound like it wasn't enjoying it much but I pressed on. After another 15 minutes of drilling I got to within about 4mm of the surface, and then the drill broke and got stuck in the hole. Luckily I managed to get it out. I've since put the part back in the Alum solution. I think another go with a 3mm masonary bit will have drilled the last bit out, but I think the thread might be beyond use. I could probably live without that bolt and use the other 5 but it is annoying me now. I'll clean it out and see what to do. Could enlarge the hole then make a plug with a flange on it and press it in from the reverse side, then drill and tap into that. Probably tap it before pressing it in just in case !
    Last edited by routercnc; 30-12-2015 at 10:48 PM. Reason: added video
    Building a CNC machine to make a better one since 2010 . . .
    MK1 (1st photo), MK2, MK3, MK4

  4. #4
    After a day there were lots of black specs and a general browny dust settled onto the part (hole now top left).
    I read something about this in an earlier post and I thought it said you had to keep it on a low light to keep it warm for it to work
    ..Clive
    The more you know, The better you know, How little you know

  5. #5
    .... it on a low heat to keep it warm for it to work
    Fixed.

    Have you tried putting more alum powder in to see if your concentration is too low?
    https://emvioeng.com
    Machine tools and 3D printing supplies. Expanding constantly.

  6. Hi Clive, Komatias,

    I'd also read about constant heat but I don't have a hot plate and using the oven/hob was not allowed so I periodically drained some off and topped it up with water from the kettle. It was wrapped in insulating cloths to keep it warm for as long as possible.

    I added about 100g of powder initially, and changed the whole lot for a new batch of 150g after a day or so. There was always some undissolved powder in the bottom even with lots of stirring which meant it was saturated at maximum concentration.

    It was working, just slowly. I think a hot plate or keeping it fairly hot would give it more chance, I'll see what I can get hold of.

    I don't know if drilling with the masonary bit would have taken 15 minutes without the Alum powder treatment or if several days in the Alum had softened it. I'm nearly through with the drill so when I'm next in the workshop I should break right through.
    Building a CNC machine to make a better one since 2010 . . .
    MK1 (1st photo), MK2, MK3, MK4

  7. #7
    Masonary bits are too blunt. You would also need to spin backwards to aid removal of the tap. I have used special carbide spade drills to remove taps. The only place in the Uk that has them is
    http://www.drill-service.co.uk/Produ...60000&Tool=377
    Seriously considering stocking some in 2016
    https://emvioeng.com
    Machine tools and 3D printing supplies. Expanding constantly.

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