. .

Hybrid View

Previous Post Previous Post   Next Post Next Post
  1. #1
    It's alive!

    Heated the angular contact bearing in oven, cooled the shaft and it dropped straight on.
    Bit of a fiddle to get the rest together, but it went ok.

    I've run it up to 3100rpm (24v) and it sounds fine. Slight noise from the bearing but I don't think that's significant.

    I also measured the runout and it's less than 0.01mm.

    Will post some more pics in a minute.

    Click image for larger version. 

Name:	DSC06918 (Medium).JPG 
Views:	4529 
Size:	149.2 KB 
ID:	3639
    Attachment 3642
    Attachment 3646
    Attachment 3643
    Attachment 3647
    Attachment 3644
    Attached Thumbnails Attached Thumbnails Click image for larger version. 

Name:	DSC06900 (Medium).JPG 
Views:	1738 
Size:	77.6 KB 
ID:	3648   Click image for larger version. 

Name:	DSC06898 (Medium).JPG 
Views:	1503 
Size:	68.7 KB 
ID:	3649   Click image for larger version. 

Name:	DSC06906 (Medium).JPG 
Views:	2537 
Size:	103.5 KB 
ID:	3650   Click image for larger version. 

Name:	DSC06895 (Medium).JPG 
Views:	1473 
Size:	112.6 KB 
ID:	3651   Click image for larger version. 

Name:	DSC06902 (Medium).JPG 
Views:	4895 
Size:	118.8 KB 
ID:	3652  
    Last edited by Jonathan; 22-01-2011 at 04:23 PM.

  2. #2
    Quote Originally Posted by Jonathan View Post
    It's alive!

    Heated the angular contact bearing in oven, cooled the shaft and it dropped straight on.
    Bit of a fiddle to get the rest together, but it went ok.

    I've run it up to 3100rpm (24v) and it sounds fine. Slight noise from the bearing but I don't think that's significant.

    I also measured the runout and it's less than 0.01mm.

    Will post some pics in a minute.
    Nice one jonathan !!!! iv waited a long time to see this beast
    it should have enough power to make a walnut wip out of your Y axis :)

  3. #3
    Quote Originally Posted by blackburn mark View Post
    Nice one jonathan !!!! iv waited a long time to see this beast
    it should have enough power to make a walnut wip out of your Y axis :)
    That makes two of us.
    Make a walnut what?! But yeah, running it off two 12v 92Ah batteries for the moment. Not got a power supply which would supply anything like enough for this. Idling at 3100rpm it consumes 94w. 45w ish at 1500 rpm... that implies almost 200w just to spin the thing at full speed let alone cutting!

  4. #4
    looks great, i love how simple these thing are :)

    Make a walnut what?!
    Click image for larger version. 

Name:	walnut whip.jpg 
Views:	3737 
Size:	5.4 KB 
ID:	3640
    walnut whip ! .... shit joke.... sorry :)

    94w
    owch, but as M250cnc phil said to me not to long ago"give your bearing a chance to run in at low (ish) speed before you start flapping about heat" or "drag" in your case

    im getting on fine using 350w 12v on my 1700w motor, i dont think you will need to throw 6000w at yours if your using it on your router
    Last edited by blackburn mark; 20-01-2011 at 08:28 PM.

  5. #5
    Quote Originally Posted by blackburn mark View Post
    owch, but as M250cnc phil said to me not to long ago"give your bearing a chance to run in at low (ish) speed before you start flapping about heat" or "drag" in your case

    im getting on fine using 350w 12v on my 1700w motor, i dont think you will need to throw 6000w at yours if your using it on your router
    I did the mount today, not the neatest of things I've made with the rotary table but it works:


    Click image for larger version. 

Name:	DSC06920 (Medium).JPG 
Views:	1759 
Size:	79.4 KB 
ID:	3654
    Click image for larger version. 

Name:	DSC06921 (Medium).JPG 
Views:	2705 
Size:	51.9 KB 
ID:	3653
    Spinning...nice effect:
    Click image for larger version. 

Name:	DSC06923 (Medium).JPG 
Views:	3073 
Size:	92.5 KB 
ID:	3655

    I ran the motor in for about 5 mins on 12v, soon got bored of that (I'll leave it running properly tomorrow). So I tried carefully grasping the motor body with some kitchen roll to protect my fingers - couldn't stall it, not even close . It merely drew 550w and about 53 amps. I'll have to think of a safer way of testing the power at higher voltages.

    I think I'll stick with the batteries for now unless anyone can point me to a 50v PSU that can deliver a LOT of current. Maybe a few of those switching PSUs people have been using for steppers on eBay...
    Last edited by Jonathan; 22-01-2011 at 04:30 PM.

  6. #6
    Quote Originally Posted by Jonathan View Post
    I did the mount today, not the neatest of things I've made with the rotary table but it works:

    (Picture tomorrow)
    I was under the impression your mill was under cnc control why the RT ?

    Quote Originally Posted by Jonathan View Post
    I ran the motor in for about 5 mins on 12v, soon got bored of that (I'll leave it running properly tomorrow).
    Its a temperature thing if it doesn't get hot just keep increasing the speed in increments.

    Quote Originally Posted by Jonathan View Post
    It merely drew 550w and about 53 amps. I'll have to think of a safer way of testing the power at higher voltages.

    I think I'll stick with the batteries for now unless anyone can point me to a 50v PSU that can deliver a LOT of current. Maybe a few of those switching PSUs people have been using for steppers on eBay...
    Sounds like mum & dad are gonna have a big leccy bill coming.

    Phil

  7. #7
    Quote Originally Posted by M250cnc View Post
    I was under the impression your mill was under cnc control why the RT ?
    I took the steppers off the milling machine and put them on the router. Didn't want to put them back just for one part. Rotary table was also the most accurate way I could make the hole for the spindle, not having a boring head.



    Quote Originally Posted by M250cnc View Post
    Its a temperature thing if it doesn't get hot just keep increasing the speed in increments.
    That's good, the bearing didn't get hot at all. ESC warmed up a little but that's all. I'll leave it running on 3100rpm for a while today and see what happens.

    Quote Originally Posted by M250cnc View Post
    Sounds like mum & dad are gonna have a big leccy bill coming.
    Hmm, didn't think of that - and nor have they :naughty:
    The batteries I'm using to power it were going to be charged from my wind turbine. If only I had space to mount it...

    I measured the runout again now it's mounted properly. I put a 10mm cutter in and measured 0.03mm about 10mm from the collet. If I put the DTI on the collet chuck itself it reads 0.01mm.

Thread Information

Users Browsing this Thread

There are currently 1 users browsing this thread. (0 members and 1 guests)

Similar Threads

  1. Diy Brushless Spindle
    By blackburn mark in forum Brushless Spindles & Motors
    Replies: 181
    Last Post: 08-06-2021, 03:50 PM
  2. Spindle motors resonable options
    By Web Goblin in forum Spindles & Drive Motors
    Replies: 15
    Last Post: 20-11-2016, 03:31 PM
  3. DIY Brushless spindle
    By booski in forum Brushless Spindles & Motors
    Replies: 2
    Last Post: 30-10-2013, 09:36 AM
  4. FOR SALE: 400w panasonic ac brushless servo motors and drives
    By gavztheouch in forum Items For Sale
    Replies: 3
    Last Post: 29-12-2011, 03:04 PM
  5. FOR SALE: Metabo 710W 230V Electric spindle, stepper motors, Tr nuts 20x4
    By Vladimir_MD in forum Items For Sale
    Replies: 3
    Last Post: 09-04-2010, 05:24 PM

Bookmarks

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •