First job was to strip the electronics completely from it. I will be using a TB6560 3 axis driver. I`ve heard nothing but BAD things about these, but I have one anyway and it`ll certainly get me going if I can avoid blowing it up.
I wanted to flip the X axis and although replacing the entire side piece would have been ideal, I couldn`t afford it and had some pieces suitable in stock. I raised the sides and used a plate to join them. It may need some supports bridging the sides later on.
After flipping the X, I could then mount a Z axis. I made the Z axis from a small leadscrew someone kindly gave me and the slides are olite 8mm ID bushes on 8mm silver steel rod slides. The rest is just plate bolted together. There is a problem in that I`ve used a flexible coupling but I haven`t "trapped" the leadscrew. This means that the Z axis compresses on the flexible coupling and moves the relative position of the axis - not good!! This is easy to correct but I haven`t done it yet.
Once i had the X flipped and raised and the Z built, I couldn`t help try it out... it is running of only 12v at the time and the noise from these small motors is horrific, I think the TB6560 is also to blame but since then I`ve jumped upto 24v and the noise is quieter.



At this point, the mill went back to its owner while we negotiated price. Other than electronics that we both agreed wouldn`t be needed, it was all replaced to original, thankfully, if he had seen the work I`d put into it I expect the price would have gone up!
Further updates to come: Now running on 24v from two ATX supplies in series, spindle connected, first door sign engraving done...all good fun! Issues: still not sorted the z axis flexible coupling issue. Is the Z axis height too big. Flex is the spindle.