Thread: Renovating a Hardinge HLV-H
Hybrid View
-
01-04-2009 #1
Hi Jonathan,
Good to hear from you:)
.. be good to see a new Schematic and even more interesting would be the New HLV that has just come out, with the servo leadscrew.
Quick question,, with regards to the brake, you are still retaining the mechanical brake solenoid. This is the way I would be doing it, but thinking about it there may be some merit in using the inverter to do the braking, what are your thoughts on that?
It's a real pity that my VFD's 'catch spinning motor' routine doesn't seem to work 'as advertised'. If it is has to speed-up the motor (i.e. when changing from low to high speed) the motor complains loudly. The high to low speed transition was flawless. (I guess it ramps down from max frequency ).
The auto transformer you are using is single phase, are you doing the same as me and feeding the inverter with 400V single phase ? and not running it at full capacity ?
I should really get some pictures of mine on this forum.... I have just got to the primer & paint stage, (lotts of dammage to my carrige gears + rebuilding the carrige feed motor + revising its electronics have taken a lot of time) Best Jon P
I'd be tempted to replace the DC motor with a smaller 3ph one and use another small VFD for power feed - It'd have a much better speed control
Sorry to here about your carriage gears. Are new ones very expensive? :(Last edited by BillTodd; 01-04-2009 at 01:18 PM.
-
01-04-2009 #2
You might consider changing the sampling frequency as an experiment. If the motor is emitting higher frequency noises, it's often a function of mechanical resonance of the windings under load.
The size of the filter capacitor on the DC bus actually has more to do with derating than the size of the diodes, though of course the diode rating has to be considered for single phase feeding of a larger capacitor bank. Most of the VFD's I've seen suggest a 1/3 derating...e.g., use a 3hp rated unit for a 2hp motor. That's consistent with the energy under the power curve for three phase versus single phase rectifier designs. The VFDs that are rated for single phase simply have a larger capacitor bank in them. If the supplied voltage from a three phase input design VFD sinks under a heavy cutting load, it is usually fairly easy to add capacitance to the unit externally to solve the problem. The risk is exceeding the current rating of the internal diodes because they are charging a heavier peak load in each cycle. It's usually not a problem for reasonable (<50%) increases in capacitance, but needs to be checked.- Mike
http://aafradio.org/
Thread Information
Users Browsing this Thread
There are currently 1 users browsing this thread. (0 members and 1 guests)
Similar Threads
-
REBUILD: Hardinge HC rebuild
By northumbrian in forum Lathe Rebuild LogsReplies: 29Last Post: 21-02-2017, 12:07 PM -
Hardinge KL-1
By pauly45 in forum Conversion Build LogsReplies: 22Last Post: 18-10-2013, 07:31 PM -
WANTED: Hardinge hlv-h or Feeler 618
By cookie in forum Items WantedReplies: 1Last Post: 26-02-2011, 09:09 PM -
NEW MEMBER: Hardinge HLV-H Lathe
By Roger Williams in forum New Member IntroductionsReplies: 1Last Post: 25-08-2009, 01:56 PM -
Hardinge HLV-H manuals
By BillTodd in forum Milling Machines, Builds & ConversionsReplies: 13Last Post: 10-02-2009, 12:22 AM
Bookmarks