Thread: Quite an Unusual one
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14-01-2016 #1

I need 5 days to finish it and could not find the time from a couple of months. Either i am on a vacation with wife, very busy with orders or tired. Hopefully very soon, as i start needing it.
left long ball screw is unmounted and the ball nut needs centering. Cause the bloody Chinese made it bigger than the drawing so it did not fit right in the rotating nut. Change one servo cable and make the enclosure box
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23-04-2020 #2
Hello Boyan.
Nice machine I have to say. Looks very stiff! How is it running these days? Do you have a lot of work for it or mostly hobby stuff?
Anyway I wanted to ask how you went about auto-tuning the axis with double servo motors (Y-axis in my eyes, not the gantry). Auto-tuning is a very nice feature in any servo motor software, but I have not figured out how to tune an axis with double servo motors.
Also how did you go about calculating the servo motor size? Perhaps you have explained this in a post somewhere, but I couldn't find it! :)
Thanks!
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23-04-2020 #3
Thanks!
I have sufficient work for the machine. Not as much as it deserves though. I make some product on it, sometimes for other people and sometimes cut letters for signs.
I tuned the Z and used same parameters on the other axis, as more or less motors a properly calculated for the loads on each axis, working at optimum.
Then one day i figured that if i move left or right motor 5mm, its not a problem as the gantry is like 2 meters. So there is play enough. Then i entered in Samsung software and limited the movement to 5mm each side and tuned the axis like that. With a short movement. I say 5mm just to be on the safe side, it could have been 10-15mm, on such a long gantry this is like nothing, before the other side tries to engage. In Real life if i switch off 1 motor i can move the gantry front/back even with one motor only .Of course autotuning stresses the thing, so better in the short safe range. Check all that range adjustment on the Z firts, so you dont bend something.
The servo motor size Jonathan or Dean helped me, its on the first pages somewhere. But basically 400 or 750W ac servo at 230vac are the thing for a machine like that. I went with 400w as ballnut is geared 3:2 so at 3k rpm of motor i am at 20k mm / min and my motor power is multiplied by 1.5 at that ratio. My motors support up to 6k rpm so ...
As far as i understand the things, Panasonic, Samsung or other brand servos are way better than the chinese ones, so if i was going with China servos would have went with 750w ones, as price is irrelevant also on the chinese servos. No big difference. But remember. All time i am talking about AC servos driven by 230VAC drives.
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21-04-2016 #4
I take it you are not going to Surface the whole bed with that cutter?!
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19-10-2016 #5
Hi boyan
are you using epoxy for y axis? if yes how use?
thank's
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08-12-2018 #6
Ok think that'll do. Maybe to be double sure sure I will also use silicone. I imagine that would be frustrating seeing your epoxy flushing in a not properly sealed hole. :-)
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26-12-2018 #7
First time i did it not entirely right. With time discovered new ways and next time i did it welded 6mm or 8mm bar stock, distance 40mm between. Have to check if it was 8mm as it may touch the Hiwin 20 block. Better read my second build log to see how i poured a couple of times epoxy on a 3m machine untill i figure the perfect way. iin short i discovered that the most important part is to make the damned dam longer like 15 cm at least than the actual machine to compensate for the shrink and that way only one bridge is enough, and the bridge must be then outside the machine. So when all dries and shrinks, the bridge will not eat from the actual ways but from the extra length. If you know what i mean
Last edited by Boyan Silyavski; 26-12-2018 at 08:22 PM.
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27-12-2018 #8
Yes thanks. I read that post already. I will follow it. I have a vacuum chamber where I can stir epoxy under vacuum. I am excited to see if it will make a difference in accuracy. Good job btw.
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02-01-2019 #9
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The Following User Says Thank You to Boyan Silyavski For This Useful Post:
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23-04-2020 #10
Sounds good that you have work for the machine!
Thanks Boyan, for all the answers.
I like your idea and it makes sense to perform auto-tuning like that.
Myself I have build log (build in real life not started yet) if you are interrested to check it out.
Anyway I was thinking about those servo sizes as well. I will take your advice and get Delta 750W servos! Perhaps also 2020 (plan was 2010 with 400W servos) ballscrews to get a crazy speed of 30-40m/min, depending on what gear ratio I choose (3:2 or 2:1).
Not sure if I ever will need that speed but nice to have some room for experimenting.
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