Next part is the Z axis stepper motor bracket.

Laying it out:
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Machining the pocket - no adaptive toolpaths I'm afraid so about 1 hour to machine this:
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Then the slot for the motor shaft:
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Small pocket to clear the boss on the front of the stepper:
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Light skim to get a level surface:
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Outer profile cut:
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I had problems here as I had the tool stick when it was about 10mm into the part. It was on one of the curves (which I think increases the chip load a bit) and I had about 2 seconds to go from hearing the problem developing to the spindle stopping rotating. I cleared the tool and thought I'd got away with it but it had obviously missed some steps as there was a ridge in the part. I let it finish, going easier on the feedrate, then homed the machine and ran some new full depth toolpaths working up to about a 0.5mm offset inward. This made the outer surface 0.5mm smaller all round, but at least it was smooth again. For this part it did not matter so I was lucky.

Machining the bolt slots was pretty quick:
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Set it on end and machined the clearance holes for mounting (thought this might vibrate but it was fine):
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Skimmed the other side down to get the final 20mm thickness:
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That will do !
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OK, so it was not 20.00 everywhere . . . !
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Counterbored to 9mm deep (DRO coming in handy here to get them to the same depth)
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Snail countersink to finish off (love these things, so much better than the star type which are a waste of time):
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Done. Worked out OK in the end:
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