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  1. #1
    Chaz's Avatar
    Lives in Ickenham, West London, United Kingdom. Last Activity: 1 Week Ago Has a total post count of 1,657. Received thanks 115 times, giving thanks to others 71 times.
    Quote Originally Posted by JAZZCNC View Post
    One other thing not mentioned or consdiered is weight.?

    The combined weight of Spindle cartridge, motor and all that concrete will most likely require some form of counter balance. Servo alone unless large KW won't be enough I think.

    My big mill has got Int40 (Same as taper BT40 with slightly different holder) spindle with 5.5Kw Inverter Motor which spins at 7500rpm and the motor alone is too heavy for one man to safely handle. The pulley alone (which uses 2 x multi V belts not HTD.!!) must weigh same as 2.2Kw spindle.

    Recently I removed the head unit from column and reckon it must weigh 500kg. There is 10" sqr 3ft long Solid steel block runs down the centre of column that counter balances it. The whole thing can be lifted up/down turning the ballscrew by hand.!!

    Click image for larger version. 

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    Yep, this is a valid concern. This is probably another reason why I will be a bit limited. That said, I could look at doing something to counterbalance - just adds some cost / time to the project.

  2. #2
    Quote Originally Posted by Chaz View Post
    Yep, this is a valid concern. This is probably another reason why I will be a bit limited. That said, I could look at doing something to counterbalance - just adds some cost / time to the project.
    Time and cost yes, but your head is going to be pretty heavy so i reckon it will be best building in some sort of counterbalance now, could be hard to add later. This is likely why bigger machines have a fixed head/column and moving X/Y bed - you cant slam the head around if there is half a ton of counterweight hanging off it ;)
    Last edited by Davek0974; 11-01-2017 at 03:48 PM.

  3. #3
    Chaz's Avatar
    Lives in Ickenham, West London, United Kingdom. Last Activity: 1 Week Ago Has a total post count of 1,657. Received thanks 115 times, giving thanks to others 71 times.
    Some pricing from Posa for reference.

    1
    Spindle for
    CNC Machining Center
    Built-in
    EMS-30
    12,000/ 15,000 RPM
    SET 1 USD4,225
    2
    Spindle for
    CNC Machining Center
    Belt Drive
    DS-BT30
    15,000 RPM
    SET 1 USD2,630
    3
    Spindle for
    CNC Machining Center
    Belt Drive
    DS-BT30
    12,000 RPM
    SET 1 USD1,840

    http://en.machine-catalog.com/adsl/O...atalog/214.htm - you can find teh details in there.

  4. #4
    Chaz's Avatar
    Lives in Ickenham, West London, United Kingdom. Last Activity: 1 Week Ago Has a total post count of 1,657. Received thanks 115 times, giving thanks to others 71 times.
    Some update after a long absence (and winter).

    Gantry is now epoxied to the main structure. Waiting for the epoxy to harden fully before taking away the jacks / hoist to see if it holds the estimated 700 kg gantry.

    Busy drawing up the proxy mount parts and did some testing with them.

    Id like to add limit switches, can I use proxy switches in series or best to go mechanical for these? I want to use all in series going to a single input in CS Labs / Mach 3.

    Click image for larger version. 

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  5. #5
    Chaz's Avatar
    Lives in Ickenham, West London, United Kingdom. Last Activity: 1 Week Ago Has a total post count of 1,657. Received thanks 115 times, giving thanks to others 71 times.
    So, an update.

    I managed to epoxy the gantry to the main body. Scary stuff this. Will some 'glue' hold an estimated 750 kg weight? Seem it does.



    Next step was to rotate the mass and remove the table as I needed access to the rails.

    Ignore the loose rails in the middle of the lower part.



    I then, with a lot of effort, lift my 300 kg 'reference' onto the rails, align and mount so that I can use this to get the epoxy set against the gantry.





    The nett result is that I have something that moves forwards and backwards that is aligned to the bottom rails and should therefore be square once moulded. I should be doing the epoxy pouring this weekend.

    Some of you might note that the reference part is only 50% of the width of the gantry. I dont have a larger reference surface and using it on its side means it will be too low.

    So two options. I can either mould this width and then use a surface plate that I have and basically overlap until I get the full width.
    Second option (and what I have gone for) is to basically put 100mm wide (the rails are only 40 but I need some extra height for the adjustment up and down) 30mm thick alu tooling plate (Eco Cast). I know its not perfectly flat but I am hoping this will be reasonable. Ill bolt this to the reference square and see how this looks.

    https://youtu.be/ZtDXA0xAFhQ

  6. #6
    Chaz's Avatar
    Lives in Ickenham, West London, United Kingdom. Last Activity: 1 Week Ago Has a total post count of 1,657. Received thanks 115 times, giving thanks to others 71 times.
    Mounted the tooling alu, a quick sweep tells me it looks to be accurate to within 0.05mm. Not ideal but not bad for a garage job.

    Around 6 coats of carnuba wax later, we are ready to pour the epoxy.









    The epoxy takes 24-48 hours to set but will leave it for the week and remove the reference table / plates to see the result. Then it will be a case of drilling holes and mounting the rails which is a pain in the backside. Not sure yet how Im going to epoxy the nuts in yet - when doing it from the top, gravity helps. On its side, not sure.

  7. #7
    Chaz's Avatar
    Lives in Ickenham, West London, United Kingdom. Last Activity: 1 Week Ago Has a total post count of 1,657. Received thanks 115 times, giving thanks to others 71 times.
    Success!

    Apart from some places that remained a bit unmixed, the rest has gone hard and is mirror smooth.

    Removed the reference frame, alu still 'stuck' to the epoxy.



    Then, a bit of prying with a crowbar and both parts are off.

    The remaining epoxy is smooth and even has the tooling marks that transfers across from the plate.

    A quick test with a straight edge confirms all is good. A quick test with the rails indicate they arent perfectly straight (This will be fixed as they get bolted down).







    Next step is to drill two holes, around 1/3 from each side and mount, get basic alignment, using reference piece for X travel height calibration. Marking the rest of the holes, drilling, then mounting with another alignment test. This takes ages as I need to go to around 26mm from memory and there are many to drill into this hard concrete.

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