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  1. #10
    It's about now that I regretted my choice of spindle. When experimenting, trying to find cutting depths and feeds that worked, I became suspicious that something, somewhere wasn't right.

    I went through the machine, looking for backlash, play or loose fasteners, but I couldn't find anything amiss - everything seemed tight. I then started clamping an indicator to various places to see how much they deflected and eventually found that firm hand pressure against the ER11 collet chuck would move it by ~0.1mm the spindle itself was only moving by ~0.01mm.

    This led on to the discovery that the spindle bearings were a) weedy and b) wedged into the end cap with a rubber boot!



    At this point, I should have cut my losses and found a different spindle. But I had a couple of spare angular contact bearings, and there seemed to be a lot of fresh air inside the front of the spindle housing...

    I drew up the original design in CAD:



    And indeed, as it seemed, there was enough space to fit in some more substantial bearings.

    The only way I could think of to locate them axially was by sandwiching the original circlip (or something in its groove) between the pair of angular contact bearings that I had:



    I had a suitable chunk of aluminium already, so the only thing I would be wasting was my time...

    I needed to get the ER11 chuck off the old spindle to get to the bearing. My word, it was on tight! I had to heat it and jack it off the shaft with a bolt through a nut held inside the ER11 collet nut. It was that tight that I stripped the threads of a normal M6 bolt and had to use a HT cap screw one instead.

    The new bearing housing and preload nut were turned up on the lathe:






    The new bits and the old bits side by side



    New bits assembled to the armature



    All I had to do now was get that ***** ER11 chuck back on. I thought I might get away with being civilised - I heated the chuck and tried to press it onto the armature using my lathe tailstock. It didn't want to know at all. I eventually resorted to brute force, and drove it back on with a hammer.



    In the process of replacing the chuck, I managed to smash up the brushes (I found out when I tried to power it up. There was a bang and a flash and all the lights went out...) Spares brushes are available from China with 3-4 weeks shipping. As I'm impatient, I ordered something close and sanded them to fit. While I was in there, I made a brass sleeve to replace the rubber bush on the rear bearing.

    Perhaps unsurprisingly, the collet chuck didn't run awfully true afterwards (maybe +/- 0.05mm). I had marked the orientation of the chuck wrt the shaft when I took them apart, but my marks were inside the motor when I put them back together, so I couldn't see them! (I don't know if it would have made much difference.)

    Anyway, it wasn't coming apart again, so any improvement would need to be made with the spindle assembled. I started thinking about how to set it up in the lathe to be able to re-cut the ER collet taper and realised that if I could support the spindle housing, I could true up the collet taper with it running in its own bearings. My fixed steady was *just* big enough to go around the new preload nut which held the housing steady so that I could re-cut the collet taper.



    The best I could get was +/- 0.01mm runout when measured on the shank of a tool clamped in the collet. (I don't have any 'before' measurements to compare it to.)

    I had measured the stiffness (compliance??) of the spindle before I took it to bits, and while there was an improvement afterwards, it was not as much as I had hoped - I was measuring ~800 N/mm before and ~2,500 N/mm after (measured at the top of the collet chuck - it would be lower at the tool tip). The stiffness of the spindle body measured next to the chuck is ~6000 N/mm (with the Z axis raised).

    It is also very temperature sensitive - the bearings tighten up when cold, so I need to run the spindle for a few minutes to warm it up before trying to cut anything. (I probably shouldn't have used aluminium for the bearing housing)

    I was hoping to be able to turn a sow's ear into a silk purse, but I think all I've achieved is to make a slightly better sow's ear.

    I recommend against following in my footsteps, but I'm running with it for the time being.
    Last edited by Misterg; 03-01-2023 at 03:23 PM.

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