. .

Hybrid View

Previous Post Previous Post   Next Post Next Post
  1. #1
    I capped all the open ends on the base and welded in a few more blind bushes where I expected to need to fix something, then keyed up the tops of the rails with some coarse paper on the sander before masking them up and doing the epoxy/glass plate thing again to level them off






    Again, the epoxy bedding seemed to work OK.




    A slightly better paint job




    And a look at progress so far.



    The Y axis carriage was made from an aluminium tooling plate offcut (ex ebay). It arrived cut nice and square, so by fixing the Y axis cars parallel to one edge, I could get the Y linear rails perpendicular to the X axis by setting the end of the plate parallel to the X axis (everything was just being roughly squared at this point).




    The linear rails are the Chinese ones I'd ordered originally (12mm x 300mm). I'd have liked them to be a bit longer and a bit heavier (even 15mm), but as I already had them, and was trying to do this on a shoe-string, it seemed a waste not to use them.

    I had trouble with the carriage binding when I tightened everything up initially, which I eventually traced to the Chinese ball bearing cars being different heights:




    I'd bought a pair of rails with 1 car each plus two spare cars from the same listing on Aliexpress. The heights depended on which rail they were mounted on, and also which way around they were fitted. By swapping them between rails and turning them end-for-end I eventually found a combination that was near enough that the carriage would run smoothly without binding. The tooling plate offcut also had a slight bow to it which didn't help. (Any height difference side to side wasn't really important as I would be aligning the gantry to the Y axis eventually.)

    I'd already ordered a leadscrew for the Y axis on spec, and as it turned out, it was too long. It was easily lopped to length with the angle grinder, but turning the end down to take the support bearing was a bit much for the mini lathe - the intermittent cuts on hardened steel turned it into a bit of a rodeo, and not something I'd like to make a habit of!




    It did it though




    I tried to cut a circlip groove in it using an HSS tool, but it (quite literally) didn't even scratch the surface. I eventually resorted to cutting the groove with a hacksaw.

    A a nice, parallel packing piece was needed to make up the space between the ballscrew nut and the underside of the carriage (stll a space in the photo) - this was just faced to length in the lathe.

    The Y axis assembled



    The support bearing for the end of the leadscrew was similar to the X axis one.

    And that was the major bits all made. :)

  2. The Following 2 Users Say Thank You to Misterg For This Useful Post:


  3. #2
    Excellent work Mr G, coming along nicely, nice and strong..
    -use common sense, if you lack it, there is no software to help that.

    Email: [email protected]

    Web site: www.jazzcnc.co.uk

  4. The Following User Says Thank You to JAZZCNC For This Useful Post:


Thread Information

Users Browsing this Thread

There are currently 7 users browsing this thread. (0 members and 7 guests)

Similar Threads

  1. Diy CNC mill-router-thing in my attic
    By Pencilfish in forum Workshop & Equipment
    Replies: 0
    Last Post: 29-11-2021, 06:18 PM
  2. Funny forum thing.....:disillusionment:
    By Voicecoil in forum General Discussion
    Replies: 4
    Last Post: 07-04-2021, 06:47 PM
  3. Replies: 11
    Last Post: 26-08-2020, 09:04 PM
  4. Trying to get this thing to work
    By GeneO in forum Machine Discussion
    Replies: 29
    Last Post: 21-01-2020, 09:29 PM
  5. Bought a laser, now there's a thing
    By Robin Hewitt in forum Laser Machines & Building
    Replies: 26
    Last Post: 25-02-2013, 07:20 AM

Bookmarks

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •