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13-01-2017 #1
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16-01-2017 #2
Boyan, thanks I think it might be a little much and also Im not real sure how it will work but I run 6inch to all my machines and have a 10hp cyclone dust collection system so I thought it would be better to have 2 4 inch tubes down to the bit rather than just one 6 inch. I will make an update on how it works once its all hooked up and the dust shoe is made/installed.
Thanks for the comments on the ballscrew/nut the sound just didnt sound great but like I said I havent ever been close up to a machine. Of course once it is cutting those sounds cant be heard.
So I decided to make a temporary spindle cooling fan adapter and get this thing cutting. So the first thing I wanted/needed to make is the dust collection adapter mold.
Heres the machine cutting for the first time.
Turned out pretty good for the first cuts, here is a final picture and the first 1/2 of the dust collection adapter laid up in fiberglass.
I learned a few things on my machine, first one was not to difficult, I needed a better tune on the Z axis. I think you can see in the movie that the Z actually moved up and down slightly through its pass, for this part it didnt really matter so I let it run and played with the tuning a bunch more and I think I get it pretty good.
The other thing is I was making ellipses instead of circles. Again this part didnt matter that much so I let it run to look into it after. So after confirming gantry to X squareness I started looking into what else it could be.
Heres what I found and looking for a little help on this, I also want to say that I really appreciate all the help the experts on this forum give and I hope this build helps others with theirs..
I put the machine on a 10 inch X movement back and forth at a moderate speed, while watching the gantry I could see a noticeable racking of the gantry. Upon stopping, the gantry comes back to square. It looks like to me that X axis slave motor/ballscrew is noticeably slower at starting. I tried to use the motor delay setting in Mach, I moved the milliseconds up (delaying the master motor since the slave seemed slower) but I could not see a noticeable change. So for all of the experts out there, is the motor delay something I should be adjusting? Or is there something else I should look into? I have confirmed all the settings in Mach on both motors are the same. I also confirmed the settings in the servo drives are the same. Any thoughts are appreciated.
Thanks
Scott
EDIT
I just looked closer at the delay, I had assumed that it was a signal delay, but as the manual says (which I should have looked at first) the motor delay is for delaying the enable signal for that output. So now I really dont know what to do.
The reason I say the slave axis seems delayed is the gantry racks as if the master motor is the only one driving it. I thought maybe the slave motor was/is not running but the fact that the gantry gets to square when it stops I think tells me the slave servo is running (resolver is bringing the system back to correct position). The servo drives output for speed match when running as well. Hope there is a good way to adjust for this delay?Last edited by Scott Damman; 16-01-2017 at 04:01 AM.
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16-01-2017 #3
Make sure both servos have exactly the same settings in the servo drives themselves. I do that by copy-paste-upload from one servo to the other in the servo tuning program. So i am 100% sure they work the same. Do so in mach 3 in motor tuning tab and make sure to hit "apply". Close. go out of mach 3, then do check again the result. Then make sure the direction of motors is set right before you rip your gantry.
Then test.Now all must work normal
About the dust, i see. You are right that dust extraction better not be choked down. I assume you will fit a kind of shoe there. Or you will extract only the fine dust not to float around in the air? I use sometimes my dust shoe only like that, without the brush attachment. Chips stay on table but no fine dust in the air.
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16-01-2017 #4
May sound obvious but if you are using pulleys are they the same size.?
If this was Step/Dir setup I'd say the Step pulse was on wrong edge but with Analog IP-A then can't happen.
Does it look like it's running out over time while cutting or is it off straight away.? . . . . It could easily be electrical noise inducing voltage on the signal lines.
This would have the same affect has being told to move fractions of inch more than should. The encoders will always bring it back to zero when homing so very difficult to see.
Does it do it without Spindle Running.?
Do you have any Line filters on the Drives or VFD.? . . . If not fit some because Servo's, esp Analog don't tolerate noise in power line very well.!
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17-01-2017 #5
Boyan, I went through all the parameters manually as the drives from BST Automation dont have a computer hookup. But I was able to confirm that all parameters are the same in the drives.
JAZZCNC
Re: First Build 5 x 12 Steel Frame CNC router
May sound obvious but if you are using pulleys are they the same size.?
If this was Step/Dir setup I'd say the Step pulse was on wrong edge but with Analog IP-A then can't happen.
Does it look like it's running out over time while cutting or is it off straight away.? . . . . It could easily be electrical noise inducing voltage on the signal lines.
This would have the same affect has being told to move fractions of inch more than should. The encoders will always bring it back to zero when homing so very difficult to see.
Does it do it without Spindle Running.?
Do you have any Line filters on the Drives or VFD.? . . . If not fit some because Servo's, esp Analog don't tolerate noise in power line very well.!
Both sets of pulleys and belts are the same and came from the same supplier.
It is more of a delay to start, i.e. the master motor starts moving and the slave starts up just slightly after (which racks the gantry). When it comes to a stop the master stop slightly before the slave bringing it back into square.
Happens whether the spindle is on or off.
One thing to note the cables are 1meter longer to that motor than the master motor. I wouldnt think that should cause this but maybe?
I think to your point it is likely noise, I found yesterday while cutting some other parts that my Y is undershooting its commanded position. I was cutting a part that was supposed to be 8 inches in Y and it is 7.85inch. When I run the Y without the spindle on and a dial indication its within 0.001inch... So I am going to have to dig into the noise.
When you say line filters on the VFD's you are talking input line filters correct? I will see if I can come up with some input line filters. Also want to dig into the grounding more and confirm that everything is hooked up correctly. I have everything grounded back to a single point in the cabinet and then that run to our homes earth ground. I am thinking of driving a separate ground rod for the machine to give it a shorter path to ground, good idea? The spindle is run with triple shielded continuous flex VFD cable, the cable shield is connected to the chassis of the VFD using a VFD cable connector, i.e. the shield is connected 360 deg to the chassis of the VFD. The VFD is then grounded back to the single point ground in the cabinet. Open to help on this!
Made some progress on the dust collection adapter first picture is the first half out of the mold and the second is the second half laid up in the mold.
Also worked on a support arm for dust collection tube. It bit overkill but it was fun to make...
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17-01-2017 #6
Again another obvious suggestion but got to be said to eliminate. Not got loose Pulley.?
Yes Input line Filters.
Did you Earth the Frame.?
Re: Separate ground rod then I'd say not because want to use the same ground that mains supply does so don't introduce ground loops. However I'm not expert on this and don't know the differences between American and UK electrics other than frequency.
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17-01-2017 #7
I appreciate all of the "obvious" questions as it is easy to overlook items when troubleshooting... Yes confirmed no loose pulleys, I also have been watching the actual belts on the servos on X (hard to watch both of course) but it looks like the master is moving before the slave. I plan to swap cables to those motors and then swap drives and find where the issue follows. I can then hopefully pinpoint, cables, drive, motor being the culprit. (or still noise)
Frame grounded and I have a ground going to the gantry and to the Z axis to make sure each part is grounded in the frame.
So the separate ground would need to be bonded back to the ground ref in our house (as I believe this is code). My thinking here would be that this ground rod would give a much shorter path to earth for the Hf noise. Not sure it would make a difference or not just something I was thinking of trying.
One question I have is about running cables in the same drag chain, I had assumed that having good shielded cables that I could run all of the cables together in the same chain. Is this a No/No?
I have been looking into line filters to try to get some ordered for the servo drives and the VFD for the spindle.
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17-01-2017 #8
Not good idea unless you know they are isolated. It's little things like this that can easily introduce ground loops. I would remove the Gantry and Z axis earths and check again.
Also don't Earth the PC chassis to the Star point. This can cause all sorts of strange happenings. The PC PSU will have it's own path back to earth so adding another affectively creates G-loop.!
If all is correct regards Grounding etc and with good wiring practices then shouldn't be problem. I do this all the time and don't have any issues.
However it's always good idea to keep some seperation of high power/frequency cables like VFD or Mains voltage in respect Signal wires. Esp if the wire runs are long which guess may be on your machine.Last edited by JAZZCNC; 17-01-2017 at 08:54 PM.
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17-01-2017 #9
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